Rohde & Schwarz SMS2 372.2019.28

 I bought this rather sought-after signal generator from a chap on Ebay where he'd described it as "faulty". It was £25 to deliver and only £45 to purchase. Sure enough, as the seller had stated, the thing came on and apparently passed its self-test but then failed to respond to its keys. In order to let it run through the short test however, the on/off switch needed to be held in the ON position (a very common fault). See my first example here.

Although the thing is decribed in R & S literature as "easy to fault diagnose", I don't find this particularly true as dozens and dozens and dozens of screws need to be removed for virtually any fault-finding.

What's puzzling is how can the thing pass its self test and be duff?

I suppose that the designers just didn't bother to test everything, leaving out at least one key parameter.

As always, looking back into the initial evidence appears to pinpoint the likely fault because during and after the initial few minutes, I should have noticed the fan was dead. Maybe, in the SMS2 version the fan is designed to run only when its hot enough to be needed? But I didn't believe this to be the case (and it wasn't) because in my first repair of an SMS equipment the fan (which should be always on) wasn't running properly either.

The first thing to tackle is the bad mains switch. Luckily these switches are very similar to a standard (old) TV mains switch and I had one in my "switches" junk box. Fitting it was a bit tricky but it was finally working. Because most SMS or SMS2 equipments will need attention to their switch I've put the following pictures below to give you an idea of the work to either fix with WD40 or to fit a new one.

 

 This is a general view of the underside of the SMS2 (the SMS is the same). The switch usually turns on but fails to lock in position. My first example responded to a squirt of WD40 but this one didn't so needed replacing. A standard old TV switch does the job. Ignore the ancillary contact set which were used for degaussing.

 

 

 

 

 Above you can see the rear panel can be unscrewed enough to allow the switch to be pulled back from its operating rod which just presses onto the switch. Note that the existing switch bracket may have different hole spacing to the replacement and so the new one will need drilling to fit the mounting holes. Before pressing the bracket tabs closed check the new bracket is facing forwards otherwise it won't fit.

It's important to note that if you use my recommended switch the solder tags are different to the original. The original has two normally open contacts across the switch body whilst mine has them front-to-back. If you connect the mains wire wrongly there'll be a loud bang when the switch is operated!

 

Below the old switch on the left and right the new switch screwed in position. Because of the position of the switch wiring right where one might grab the chassis to turn it over it's essential to refit the protective plastic cover. As the original no longer clipped into place I superglued it using baking power to make the result more robust.

 

 

 

 I said previously the job was "a bit tricky" and by that I meant that the throw of the two switches was different. The rod needs to have enough movement both to comfortably operate the engage mechanism and to fully disengage it. My solution was to wind four turns of thin bare wire though the rod's end slot. The wire blocks the switch from sinking too deeply into the rod end and with just the right number of turns of wire the engage/disengage works fine. To stop the rod springing off when turning the switch off I applied a little superglue to the inside of the rod end before finally pushing it into place.

 Having got the signal generator to turn on reliably I turned my attention to the main fault of dead switches after self-test. I thought the most likely problem might be the power supply (perhaps a missing or low voltage) so I removed lots more screws and angled the chassis so I could test bits of it.

The SMS2 is not easy to work on as it's heavy and has no convenient handles etc to shift it around. The circuit boards are mainly inside a screened box so the box top needs to be removed if one of the boards needs to be detached. Clues to the circuitry are given on the screened circuit board box top and bottom covers, but one needs a copy of the servicing manual to make sense of the markings. This example still has its extender board screwed to the screening cover which is nice.

 

 Turning first to the PSU power regulator transistors as I'd decided to test these for shorts or leakiness.

 

 

There are also two power rectifier diodes sharing the heatsink (those two large nuts hold them in place).

Those aluminium bushes support a pair of protective metal covers because the transistor bodies are at varying DC potentials.

 

 The mechanical designers had clearly liaised with the electrical engineers and devised a rather odd arrangement of fitting the regulators (3 x 2N3055 + LM7915)

 

This involves the use of a (third) pin pressed from a plate which pressure-mates with the undersurface of each TO3 device.

A set of four 3-pin sockets are fitted to the PSU circuit board and these allow the TO3 devices to be pulled out so the circuit board can be detached from the case.

 

Click the picture to show enlarged power supply schematic

 

 I removed the four devices and all seemed to be OK, however a little later I checked continuity between the four sets of sockets and found to my surprise a dead short between the sockets for the control pin and output pin of the LM7915 with both grounded. The PSU circuit reveals the control pin to be common to a set of four DIL chips and so these connections plus the neg 15 volt rail (the LM7915 output pin) is grounded.

The fault must be either within the PSU board at one of the four DIL chips or, most likely, a dead short on the neg 15 volt rail.

Of course the fan (which is dead and should have pointed to the fault) is driven from the neg 15 volt rail. The fan itself is not bad because it's driven via a 39 ohm resistor and therefore is not responsible for the short-circuit because the short has virtually zero ohms to ground and not 39 ohms.

I guess I should now look to see if the problem lies in the PSU board itself or one of the many circuit boards (below) or any of the other parts within the SMS2, Whichever is shorting the neg 15 volt supply to ground should be identifiable by disconnecting each in turn to see which removes the short.

Initially I attempted to remove the first of the circuit boards but I found it to be so stiff I left it in place. The reason being that any plastic parts such as the coloured levering mechanisms for the circuit boards will now be brittle with age (I think this example dates from 1984 making it 40 years old in 2024).

I'd broken many similar levers in my Hewlett Packard signal generator so decided to check alternatives first which turned out to be a stroke of luck.

See later for more on this topic.

 

 

  Before attempting to extract the circuit boards I unplugged both the 24-pin (grey) and 16-pin (K30 blue) DIL connectors from the PSU board.

 

Thankfully the short on the neg 15 volt output proved to be present at one of the mating plugs on the disconnected cables (meaning I could leave the blameless PSU board in place).

 

 

 I discovered the short to be between Pin 8 and Pin 10 of the 16-way lead K30 which, in the SMS2, terminates at a small metal box above the fan. The box is labelled "SMSB2" and is the additional optional part which provides the extended coverage from 520 to 1040MHz. Looking in the manual I found the box contains two circuit board assemblies.. a frequency doubler and a switch. These are coupled by a few gold plated pins and are mounted together on the front panel of the box. I removed the panel and separated the boards as you can see in the pictures below.

 

 

 The SMSB2 box is screwed to a rear-mounted heatsink and secured by four screws to the side of the chassis. To access two of these you'll need to detach the metal plate fastened to the chassis by four countersunk screws concealed by the end tongues of the earthing strips. The connectors were detached with a 6mm spanner. A single grey wire also needed cutting from an adjacent metal box mounted at the side.

 

 
   

 The twin circuit board assembly was unscrewed (four tiny screws plus a coax plug) and pulled from the box then the switch circuit board was detached from the assembly.
 

 Click the picture to see the larger RF Switch schematic

 

 

 

 

  Once removed from the panel and the boards separated I found the neg 15 volt rail was connected to only the "switch" board where it's wired to a set of op-amps and a relay driver. Also present across the neg 15 volt rail were three small capacitors. Presumably either one of the chips or one of the capacitors has failed. The easiest way to discover the culprit was to apply neg 15 volts (correctly) across the circuit and see what gets hot. It's important to ensure the test voltage has correct polarity in case the short disappears.

 I connected my bench PSU set to a few volts to the neg 15 volt input on the Switch board and cranked up the current limiter but 3A didn't really do very much. The reason being a really dead short will have very little resistance so any power will most likely be taken by tracking. I had a couple of options. I could remove each component wired to neg 15 volts in turn or just increase the current instead. I chose the latter, connecting a 12 volt battery (in pretty poor condition) instead of the current limited PSU and there was an immediate smell of burning. None of the components was even warm, but the very thin track from the neg 15 volt input pin had burnt up. Mission accomplished though because the burnt track ended at C5, a 1.5uF capacitor and after removing this I found it was short-circuit.

 

There seems to be rather a lot of these in the SMS2 so let's hope the failure was an isolated incident! Sometimes one comes across a really stressed tantalum connected back-to-front (eg in my Wavetek 2407).

I fitted a 22uF miniature electrolytic (I'd misread the figure as 15uF but it's only a decoupler so will be OK!) and reassembled everything.This was no mean feat and involved securing many dozens of screws as well as refitting lots of sub-miniature RF connectors. Note these take a 6mm spanner.

 
 

After completing the reassembly I powered the SMS2 and was rewarded with a longer self-test followed by a new display including an indicated (correct) RF output level of -137dBm. All the front panel buttons seemed to work (I set the frequency to the 2m band and checked the modulation figures lit up). The next step is to check the RF output etc and fit a couple of new plastic button caps.

 

 

 Earlier I mentioned brittle plastic affecting the SMS2.

When I was refitting the three 2N3055 transistors and the LM7915 voltage regulator I found it a bit awkward. Once the insulating pad and the metal plate carrying the pin (connected to the device case) are in place you'll need to twist them so that their holes line up perfectly with the three motherboard sockets before inserting the device. You should be able to feel some resistance as the two device pins engage with the motherboard sockets. When you're confident the devices are plugged in you need to carefully insert the blue plastic insulating tubes. I found that about a third of these blue tubes broke into pieces. Once the final fixing screws were tightened one or two cracked as the screws were tightened fully. Fortunately I have plenty of spares and I was able to finish the job.

Once all four devices are tightened up check continuity between each screw head (=ground) and the device case to ensure there isn't a short to chassis. In addition, the case of my particular LM7915 had a different shape to the standard TO3 case and the fixing screw heads were exceedingly close to the case. To increase the spacing I added a small washer under each screw head. The washer diameter has to be no bigger than the top ring of the tube otherwise this can short to the case especially if the plastic tube degrades and squashes.

 

 

 

 One of the repaired brittle plastic feet which had suffered in shipping.

 

 

 

 Here's a tip to avoid something that might be a problem if parts are not reassembled properly.

In order to repair the switch board the SMSB2 box needs to be detached from the chassis.

At the rear is a large finned heatsink which mates with the separate RF module screwed to the back of the assembly. The heatsink is secured by two screws and of course needs to be removed in order to detach the SMSB2 from the chassis.

You can see on the side of the case (top of picture) four fixing screws, two of which were hidden by the aluminium strip sitting to one side.

The correct re-assembly procedure should be to tighten the four screws only after fitting the heatsink and its conductive paste. Once the heatsink is fully tightened, and only then, should the four fixing screws be tightened otherwise the finned heatsink may not be in proper contact with the RF module.

At the same time as the box is refitted to mate with its heatsink the coax plug (ST1) must fit snugly under the lip of the chassis.

 This instruction sheet was included

 

 Next, I need to compare my older SMS front panel board with that from the SMS2 to confirm they're identical so I could test it. They're both marked "302-7911" and look identical and to do this the front panel has to be removed to detach the display board.

The procedure isn't too tricky. The four countersunk screws are removed and the plastic front comes off. Then the on/off switch operating rod has to be pulled off the switch. Next the solid coax lead to the rear of the equipment has to be freed leaving it attached to the front panel together with the flexible coax lead which just pulls off as it uses a two pin push-on connector. There are four small screws fastening the circuit board to the backing plate and a few plastic locating clips which respond to squeezing with pliers then two flat cables to detach.

Each cable is terminated with a 16-pin DIL header. One just pulls off but the other requires the end circuit board to be pulled out an inch or so. Note the orientation of the two cables otherwise either could inadvertently be re-inserted back-to-front and also note the way the pair of extraction levers work so the board can be refitted.

The SMS signal generator with the bad display which has been parked in the workshop waiting for inspiration has either a microprocessor problem or a duff display panel. Now I know it's the former because the SMS display panel worked perfectly in the SMS2.

Both panels had missing push buttons caps but as these were different to those on the SMS2 panel, I just fitted the "2" and "RCL" caps to the SMS2 board.

 

 Now I'm going to see if what comes out of the RF socket lines up with the display.

Click to see this described on the next page
 
 

 pending

 

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